The stock for the cam ring was a piece of heavy-wall 4142 tubing, 3.25″ x 2.0″ in the annealed condition. You can used pre-hardened material, but if you do, you’ll need to anneal it before re-hardening and tempering.
Hodgson Part 014/015, Gears and Assembly
Hodgson Part 013, Jackshaft
I’ve mentioned before that obtaining quality material is one of my biggest problems here in China. Well, a corollary to that is that when I do have material, it’s probably not in the easiest-to-use form. For the jackshaft, I used a drop from a piece of 416 stainless plate that had been hardened to Rc35.
Hodgson Part 012, Cam Retainer Plate Spacers
Hodgson Part 009/110, Cam Pad Support and Retainer Pad
To save myself a little work, I used some stainless steel 6-32 hex threaded circuit board stand-offs to make the Cam Pad Supports. The spacers I bought were 18-8 SS, Male-Female, 1/4″ Hex, 6-32 Screw Size from McMaster-Carr, P/N 91075A444.
Hodgson Part 008, Cam Retainer Plate
Hodgson Part 007, Front Cover
The front cover started life as a 125mm diameter by 300mm piece of Aluminum 7075-T6. I bought a stick of this long enough to make the cover, crankcase, rear seal plate, air guide, impeller, and a few fixtures. The diameter was needed to accommodate the crankcase so I did end up wasting a little material on the other parts.
Hodgson Part 005, Bearing Retainer Plate
After almost a 2-year hiatus, I was able to restart the Hodgson project. I have a small machine shop in the lab where I work at Harvard so I have a little opportunity to play on nights and weekends.
I used a piece 2″ x 2″ square of 0.125″ of Aluminum 7075-T6 plate to make the front bearing retainer. A 3/8″ hole was drilled in the center of the piece to mount it to a scrap tooling plate in the mill vise, and the center of the part was zeroed.
Quorn Part 200, Wheelhead Collar
Quorn Part 104, Wheelhead Column
I had a slight problem when making my wheelhead column. I couldn’t find any competent machine shop with a 4-axis CNC mill to run the spiral groove. So, I needed to come up with a way that I could do it myself with the manual machines I had at my disposal. My gearhead lathe couldn’t cut a 2TPI thread so I had to find a way to make this part on the mill.